I'd be for getting ahold of Glen and asking for his thoughts. I just went out to take a peek at the dome of the piston in my GSS and it looks alright, but I don't have it on a bottle either.
The head has been completely reshaped, its a 2mm part of the squshband on the intake side that is hitting the piston, it looks like it was machined slightly off center.
My guy is gonna put it in a mill and cut off the offending bit of ally
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok
britincali wrote:Glen decked the cyl last time it popped the gasket and cracked the piston, and no the piston aint in backwards
ya piston is right i just double checked with mine. when i had that cylinder it was supposedly brand new, i dont see how it could be cracking pistons. whats the head look like ?
Where the squishband meets the flat surfce of the head there is a small lip from say 12oclock to 3pm where it wasnt quite centered when machined, it wasnt an issue when I got the motor from you as IIRC you ran the fatter cometic gasket, when I put it together I used the thin single layer honda jobbie then after the piston cracked I had the head/barrel decked which compounded the problem and gave it an even bigger hit.
Im gonna get the head back tomorrow from the guy removing the bit of material then reassemble it with a copper headgasket and go from there.
Crank feels tits BTW.
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok
It blew the headgasket bigtime last trip to dumont, it was leaking coolant all the way around. It lasted pretty well tho as this was the 3rd trip with probably 20 gal of gas and 10lb of juice total.
When I pulled the head you could see it had been going inside and out as there were tracks on the gasket and rust on the sleeve.
I dint feel it hitting, it probably dented the piston the first time I fired it.
Gotta love self race clearancing
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok
britincali wrote:It blew the headgasket bigtime last trip to dumont, it was leaking coolant all the way around. It lasted pretty well tho as this was the 3rd trip with probably 20 gal of gas and 10lb of juice total.
When I pulled the head you could see it had been going inside and out as there were tracks on the gasket.
I dint feel it hitting, it probably dented the piston the first time I fired it.
hey, i just noticed this post and was trying to explain it in another! that piston is proud to change the port timing of the jug! I've had to use stock 91+ heads and thin cometic or oem head gaskets, or 90- heads with the thick 88 style gasket to achieve the right compression!
brit read this. says if your squish velocity is wrong it can break the piston, maybe your squishband was wrong design ?. piston hitting the head may have been the culprit also. im not sure shaving the cylinder is helping either, maybe you need 2 base gaskets now
I'm no expert but if I were running nitrous I would want to keep my compression but make sure my piston to head clearance was .050 or more. Since your motor was probably set up just to run gas before the clearance was tighter. Everything expands at a greater rate running the juice but you probably knew this. It's probably a bit of an art to cutting a nitrous dome because you want to keep your compression up, you want to keep detonation down and squish band width and angle comes into play but you want a larger piston to squish clearance so when you hit the juice for a prolonged period it doesn't expand everything and hit. I would have someone cut the head that has prior experience.
Its come to a point where I can't trust anyone to do anything right anymore, the gasket I ordered from the copper gasket "pro" is fuked up, the muppet that was gonna fix the head hit it with a dremel (I could have done that and done a better job). So tonight im gonna sit down with the trusty dremel and fix all the fuked up shit myself.
Im fukin hot as hell this morning, if you want something doing right do it yourself.
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok
The offending bit of material is like a sliver of moon about 2mm thick, the dipship machinist removed most of it with his trusty dremel but there is still some material left. Im gonna hit it tonight and clean it up, im re-using the stock gasket with a heafty bead of 1211.
It just sux that between the head and the gasket in $45 out for complete shit work
It'll get done.
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok
hey, if you want, call my buddy dewayne, he cut my head and he is absolutely meticulous.
Trust me, there IS a reason I do almost everything myself besides being a cheep asshole
'09 kx450f 4-Poke
Gen-4 trail bike --SOLD--
Gen-3 badass trail/mx bike --SOLD--
Gen-1 built dunes bike --SOLD--
'05 klx110 --SOLD--
'95 pw80
pstoffers wrote:Put a stock head on it!!!!!!!!!!! And let'er buck.......
Ive got one in the garage and Ive been seriously considering it, the only question is drill the head for the bigger studs or put old studs back in the jug and buy a new gasket. ?????
Coolness list by 90cr500guy
Bob's = 50/50
Cepek = cool
Solidbro = cool
Brit = loser
Stoffer = 1 up from Brit
MFDB = cool
Danny = ok